Woody
12-05-2009, 01:48 PM
Our first trip with the new coach was interesting. Left Maine and noticed a marked decrease in power, no turbo boost, in NY state. Called Prevost who referred us to Atlantic Detroit Diesel in Lodi, NJ.
Limped the last 100 miles to them and they were super. Dropped everything and took the next 3 days and lots of $ finding:
EXHAUST OUT OF TURBO – CLAMP BROKEN
TURBO FLEX PIPE INTO HOT SECTION BROKEN, PORT SIDE
OIL LINE TO TURBO LEAKING ONTO HOT PIPE AND TURBO HOT SECTION
STBD EXHAUST MANIFOLD BROKEN – AFT STUD TIGHTENED DOWN TOO HARD BREAKING CASTING
SENSOR UNATTACHED
WIRES BOKEN
STBD EXHAUST MANIFOLD GASKET BLOWN
STBD EXHAUST MANIFOLD BROKEN – FWD STUD TIGHTENED DOWN TOO HARD BREAKING CASTING, MANIFOLD IMPROPERLY INSTALLED
PORT EXHAUST MANIFOLD GASKET BLOWN
PORT EXHAUST MANIFOLD BROKEN – AFT STUD TIGHTENED DOWN TOO HARD BREAKING CASTING, MANIFOLD IMPROPERLY INSTALLED
TURBO ITSELF MIS-MOUNTED, NEEDED TO BE ROTATED ABOUT 10 DEGREES SO THAT EXHAUSTS WILL MATE PROPERLY
COOLANT LEAK INTO ENGINE OIL – POSSIBLE CRACKED HEAD
WITH VALVE COVERS OFF FOUND THAT NONE OF THE WIRES CONNECTING THE JAKE BRAKE SOLENOIDS WERE ATTACHED, GOOD REASON FOR MY LACK OF JAKE BRAKES
What a wonderful day with the new engine - the Prevost was great.
After the repair we had far more power - the problem was not new!
Thought you all would enjoy my joys of new ownership.
Limped the last 100 miles to them and they were super. Dropped everything and took the next 3 days and lots of $ finding:
EXHAUST OUT OF TURBO – CLAMP BROKEN
TURBO FLEX PIPE INTO HOT SECTION BROKEN, PORT SIDE
OIL LINE TO TURBO LEAKING ONTO HOT PIPE AND TURBO HOT SECTION
STBD EXHAUST MANIFOLD BROKEN – AFT STUD TIGHTENED DOWN TOO HARD BREAKING CASTING
SENSOR UNATTACHED
WIRES BOKEN
STBD EXHAUST MANIFOLD GASKET BLOWN
STBD EXHAUST MANIFOLD BROKEN – FWD STUD TIGHTENED DOWN TOO HARD BREAKING CASTING, MANIFOLD IMPROPERLY INSTALLED
PORT EXHAUST MANIFOLD GASKET BLOWN
PORT EXHAUST MANIFOLD BROKEN – AFT STUD TIGHTENED DOWN TOO HARD BREAKING CASTING, MANIFOLD IMPROPERLY INSTALLED
TURBO ITSELF MIS-MOUNTED, NEEDED TO BE ROTATED ABOUT 10 DEGREES SO THAT EXHAUSTS WILL MATE PROPERLY
COOLANT LEAK INTO ENGINE OIL – POSSIBLE CRACKED HEAD
WITH VALVE COVERS OFF FOUND THAT NONE OF THE WIRES CONNECTING THE JAKE BRAKE SOLENOIDS WERE ATTACHED, GOOD REASON FOR MY LACK OF JAKE BRAKES
What a wonderful day with the new engine - the Prevost was great.
After the repair we had far more power - the problem was not new!
Thought you all would enjoy my joys of new ownership.