Joe Cannarozzi
08-18-2007, 07:15 PM
Here is a project probably very few of you will ever need done.
Our fridge was 2-way, a/c d/c, and not working when we bought our bus. For that reason plus the opening for it was predetermined and we wanted the versitility of propane that is what we went with. 2-way, but 12v/propane this time. The new one is slightly taller but the same width and depth so all that was nessessary to get it in was to raise the bottom of the upper cab. and shorten the doors. Someware in the archives there is a post that covered that project, who would have guessed:rolleyes:
I have finally gotten around to cutting an opening in the bus for the lower outer access door/louvers so now it is finally installed correctly and we do not have to pull it to winterize the ice-maker or service the unit. Up until now it drew air from inside the bus, from underneath the fridge (I shimmed it up 1 in.), that can now be sealed up as well.
1542
Plywwood and spray insulation removed.
1543
I used a 4in angle-grinder with a razor-thin grinding disk to cut the opening and notch the struts. If anyone has not had the opportunity to use these razor thin grinding disks I gotta say these things are the best invention since sliced-bread. I'm continually finding new uses and using them more frequently for a whole variety of projects. Check-um-out.
1544
In an attempt to keep as much structural integraty as possible I chose to notch these strutts insead of removing them. I'm concidering attatching some 1in. angle to the backside of these to re-support what I have cut out. They still seem VERY solid, we'll see.
1545
1546
I have to p/u some stainless flat head screws and a can of black plastic paint for the door and frame.
The chiminy, that is created by false backs in the upper cabinates, needed to be expanded/redesigned too. I think the converter compramised here cause the roof deck is directly above that location but they did it WRONG, it was too restrictive hurting the fridge preformance. I figured out a better solution and as I reassemble that I'll document it and post that tomorrow.
Believe it or not I AM getting close to having everything back on line.:)
Our fridge was 2-way, a/c d/c, and not working when we bought our bus. For that reason plus the opening for it was predetermined and we wanted the versitility of propane that is what we went with. 2-way, but 12v/propane this time. The new one is slightly taller but the same width and depth so all that was nessessary to get it in was to raise the bottom of the upper cab. and shorten the doors. Someware in the archives there is a post that covered that project, who would have guessed:rolleyes:
I have finally gotten around to cutting an opening in the bus for the lower outer access door/louvers so now it is finally installed correctly and we do not have to pull it to winterize the ice-maker or service the unit. Up until now it drew air from inside the bus, from underneath the fridge (I shimmed it up 1 in.), that can now be sealed up as well.
1542
Plywwood and spray insulation removed.
1543
I used a 4in angle-grinder with a razor-thin grinding disk to cut the opening and notch the struts. If anyone has not had the opportunity to use these razor thin grinding disks I gotta say these things are the best invention since sliced-bread. I'm continually finding new uses and using them more frequently for a whole variety of projects. Check-um-out.
1544
In an attempt to keep as much structural integraty as possible I chose to notch these strutts insead of removing them. I'm concidering attatching some 1in. angle to the backside of these to re-support what I have cut out. They still seem VERY solid, we'll see.
1545
1546
I have to p/u some stainless flat head screws and a can of black plastic paint for the door and frame.
The chiminy, that is created by false backs in the upper cabinates, needed to be expanded/redesigned too. I think the converter compramised here cause the roof deck is directly above that location but they did it WRONG, it was too restrictive hurting the fridge preformance. I figured out a better solution and as I reassemble that I'll document it and post that tomorrow.
Believe it or not I AM getting close to having everything back on line.:)